Control Tower

HDD Operations Overview

5 Active Jobs
3 / 2 Drilling / Reaming
45 / 23 Deployed / Available
8 Equipment Due Inspection

Active Operations

USA

Recent Activity

Houston Pipeline - Run 3 Complete 15 min ago
Denver Crossing - Reaming Started 2 hours ago
Motor MTR-015 - Inspection Due 4 hours ago
Phoenix Install - Job Complete Yesterday
New route planned - Dallas River Yesterday

Quick Actions

HDD Route Planner

Left click to add start point, way points and end point. Right click to finish before hitting View Cross Section

Route: 0 m

Buildings: 0

Waterways: 0

Roads: 0

Railways: 0

HDD Borehole Parameters

From horizontal (Inc: 78°)
Surface or underground
From horizontal (Inc: 102°)
Maximum depth below entry
Above bore path
Curvature limit
Curve shape

Plan View

Section View

Live Operations

Real-time monitoring of all active HDD operations

5 Active Jobs
4 On Schedule
1 Delayed
68% Avg Progress
87% Equipment Util.

Houston Pipeline Crossing

Texas Energy Corp
Drilling
45% Complete
Run 3
Days 12
MD 2,450 ft
ROP 125 ft/hr
Inc 12.5°
Azi 275°
TF 45°
Depth 35 ft

Denver River Crossing

Colorado Gas & Electric
Reaming
78% Complete
Pass 2 of 3
Days 18
MD 3,200 ft
Pull 85 klbs
Hole Size 24"
Product 16" Steel

Phoenix Highway Crossing

Arizona Water Authority
Drilling
32% Complete
Run 2
Days 5
MD 890 ft
ROP 95 ft/hr
Inc 8.2°
Azi 182°
TF 90°
Depth 22 ft

Dallas Creek Install

North Texas Pipeline
Standby
55% Complete - Waiting on Parts
Run 4
Days 15
MD 1,850 ft
Delay 2 days

Seattle Bay Crossing

Pacific Northwest Utilities
Reaming
92% Complete
Pass 3 of 3
Days 22
MD 4,100 ft
Pull 120 klbs

String Builder

Configure drill strings and reaming assemblies

Components

PDC Bit
12.25" PDC Bit 5-Blade, 16mm cutters
Roller Cone Bit
12.25" Tricone Bit TCI inserts, sealed bearing
Mud Motor
9-5/8" Mud Motor 1.5° bend, 400-600 GPM
MWD Tool
MWD/Gamma Tool Real-time surveys
Non-Mag Collar
Non-Mag Collar 31 ft, Monel
Drill Pipe
5" Drill Pipe S-135, 19.5 lb/ft
Crossover Sub
Crossover Sub 4-1/2" IF x NC50
Hole Opener
24" Hole Opener Roller cone, 4-cutter
Low Torque Reamer
18" Lo-Torque Reamer 3-cone, reduced drag

Current String Configuration

Drill Pipe
5" Drill Pipe 2,232 ft
Non-Mag Collar
NM Collar x3 93 ft
MWD Tool
MWD Tool 32 ft
Mud Motor
9-5/8" Mud Motor 28 ft
PDC Bit
12.25" PDC Bit 0.5 ft

String Specifications

2,385.5 ft Total Length
48,250 lbs Total Weight
12.25" Max OD
3.5" Min ID
4-1/2" IF Connections
8-15k lbs Rec. WOB

Engineering Calculations

Hydraulics, torque & drag, and pullback force modeling

Drilling Fluid Properties

ppg
sec/qt
cP
lb/100ft²
lb/100ft²
lb/100ft²

Borehole & String

in
in
in
in
ft
ft

Operating Parameters

gpm
psi
psi
in²

Hydraulics Summary

1,245 Pump Pressure (psi)
OK
168 Annular Velocity (ft/min)
OK
Good Hole Cleaning
OK
9.6 ECD (ppg)
OK

Pressure Distribution

Bit Jets 345 psi
Motor 350 psi
Drill String 295 psi
Annulus 255 psi
Total System Pressure: 1,245 psi (255 psi margin)

Annular Velocity Profile

Min: 120 ft/min 250 200 150 100 50 ft/min 0 500 1000 1500 2000 ft

Friction Factors

-
-

String Properties

lb/ft
lbs
-
ft

Torque & Drag Results

12,450 Surface Torque (ft-lbs)
OK
38,500 Push Force (lbs)
OK
52,200 Pull Force (lbs)
OK
45,800 Rotate Off-Bottom (lbs)
OK

Torque & Drag vs Measured Depth

60k 45k 30k 15k 0 Force (lbs) 0 600 1200 1800 2450 Measured Depth (ft) Pull (Trip Out) Push (Trip In) Rotating

Product Pipe Properties

in
in
lb/ft
lbs

Pullback Conditions

in
x
ppg
-

Pullback Force Analysis

78,450 Total Pullback Force (lbs)
47% of Safe Pull
34,790 Pipe Weight Component (lbs)
-12,340 Buoyancy Effect (lbs)
28,500 Frictional Drag (lbs)
15,200 Hydrokinetic Drag (lbs)
12,300 Capstan Effect (lbs)

Pullback Force vs Distance

Safe Pull Limit: 165,000 lbs 180k 120k 80k 40k 0 Pull Force (lbs) 0% 25% 50% 75% 100% Pullback Progress 78,450 lbs

Safety Factors

Tensile Strength
47% utilized
Rig Pullback Capacity
31% of 250,000 lbs
Collapse Resistance
22% utilized

Asset Management

Track equipment inventory and deployment status

45 Deployed
23 At Base (Ready)
12 Ready to Deploy
8 Due Inspection
5 In Repair
Asset ID Type Description Status Location Hours Run Next Inspection
MTR-001 Motor 9-5/8" Mud Motor 1.5° Deployed Houston Pipeline 245 Apr 15, 2024
MTR-002 Motor 9-5/8" Mud Motor 2.0° Available Houston Base 180 May 22, 2024
BIT-015 Drill Bit 12.25" PDC 5-Blade Deployed Denver Crossing 82 -
RMR-003 Reamer 24" Hole Opener Due Inspection Houston Base 420 Overdue
GYR-001 Survey Tool Gyro Steering Tool Deployed Phoenix Crossing 156 Jun 1, 2024
MWD-004 Survey Tool MWD Gamma In Repair Service Center 512 -
MTR-008 Motor 7" Mud Motor 1.15° Available Denver Base 95 Jul 10, 2024

Crew Planner

Manage crew assignments and scheduling across all active rigs

24 Total Crew
18 On Location
6 Off Rotation
3 Changes This Week
5 Active Rigs

Crew Schedule - April/May 2026

Rig / Crew
Week of Apr 14
MTWTFSS
Week of Apr 21
MTWTFSS
Week of Apr 28
MTWTFSS
Week of May 5
MTWTFSS
Houston Pipeline Drilling
Driller
Mike Johnson
Tom Wilson
Locator
Sarah Chen
Dave Miller
Helper
Jake Rodriguez
Dallas Crossing Reaming
Driller
Bill Thompson
Chris Anderson
Locator
Maria Garcia
Helper
Luis Hernandez
Kevin Brown
Phoenix Water Main Drilling
Driller
Robert Davis
Locator
Amy White
Jennifer Lee
Helper
Marcus Taylor
Denver Gas Line Standby
Driller
Waiting
Steve Martinez
Locator
Waiting
Paul Jackson
Helper
Waiting
Ryan Clark
Austin Fiber Install Drilling
Driller
James Wilson
Locator
Emily Scott
Helper
Daniel Moore
Driller
Locator
Helper
Crew Change

Repair & Maintenance

Tool tracking, R&M workflow, and equipment readiness

127 Deployed
+3 this week
14 In Inspection
Avg 2.1 days
8 Awaiting Parts
-2 from last week
11 In Repair
4 critical
6 In QC
Ready soon
23 Ready to Deploy
+5 this week

R&M Cycle Time (Days)

0.8
Return Transit
2.1
Inspection
3.2
Awaiting Parts
2.8
Repair
0.5
QC
Average Total Cycle: 9.4 days -1.2 days vs last month

Critical Priority Items

MTR-004 9-5/8" Mud Motor
Urgent - Stator Damage
Needed: Houston Pipeline (Apr 28)
MWD-002 MWD Gamma Tool
Awaiting Board
Needed: Dallas Crossing (May 1)
RMR-008 24" Hole Opener
Bearing Replacement
Needed: Phoenix Water (May 3)
BIT-015 12.25" PDC Bit
Cutter Inspection
Needed: Austin Fiber (May 5)

Parts Inventory Alerts

Motor Stators (9-5/8")
2 in stock
Reorder placed - ETA May 2
MWD Pulser Boards
0 in stock
Backordered - ETA May 8
Sealed Bearing Assemblies
3 in stock
Reorder required
PDC Cutter Inserts
24 in stock
Stock OK
Returned from Job 5 items
MTR-007 Mud Motor
9-5/8" 1.5° Bend
From: Houston Pipeline Arrived: Today
Hours: 245
BIT-022 PDC Bit
12.25" 5-Blade
From: Dallas Crossing Arrived: Today
Footage: 2,450 ft
COL-011 Collar
Non-Mag 31'
From: Houston Pipeline Arrived: Yesterday
Hours: 312
Inspection 4 items
MWD-003 Survey Tool
MWD Gamma
Tech: Mike R. Started: Apr 21
MTR-004 PRIORITY
9-5/8" Mud Motor
Tech: John S. Started: Apr 20
Suspected stator damage
Awaiting Parts 3 items
MWD-002 Survey Tool
MWD Gamma
Needs: Pulser Board
ETA: May 8 (Backordered)
RMR-008 Reamer
24" Hole Opener
Needs: Bearing Assembly
ETA: Apr 26 (In Transit)
In Repair 4 items
MTR-012 Mud Motor
7-3/4" 1.15° Bend
Stator Replacement Tech: Carlos M.
75%
BIT-018 PDC Bit
9-7/8" 6-Blade
Cutter Replacement x4 Tech: David L.
40%
QC / Testing 2 items
MTR-009 Mud Motor
9-5/8" 1.5° Bend
Flow Test
Pressure Test
Final Inspection
MWD-005 Survey Tool
Gyro Steering
Calibration
Signal Test
Battery Check
Ready for Release
Ready to Deploy 6 items
MTR-006 Mud Motor
9-5/8" 1.5° Bend
QC Passed Apr 21
BIT-025 PDC Bit
12.25" 5-Blade
QC Passed Apr 20
RMR-003 Reamer
24" Hole Opener
Assigned: Dallas Crossing
Ship: Apr 26
8 Outbound to Jobs
5 Returning to Shop
12 Scheduled Shipments

Outbound to Jobs

SHP-2024-0892 In Transit
Houston Shop Dallas Crossing
MTR-006, BIT-025, COL-008 (3 items)
ETA: Today 4:30 PM
Carrier: Company Truck #12 Driver: Tom Williams
SHP-2024-0895 Scheduled
Houston Shop Phoenix Water Main
RMR-003, MTR-011, MWD-005 (3 items)
Departs: Apr 26, 6:00 AM
SHP-2024-0898 Loading
Houston Shop Austin Fiber Install
BIT-019, COL-015, COL-016 (3 items)
Departs: Today 2:00 PM

Returning to Shop

SHP-2024-0890 In Transit
Houston Pipeline Houston Shop
MTR-007, BIT-022, COL-011 (3 items)
ETA: Today 11:30 AM
Reason: Job Complete - Routine R&M
SHP-2024-0893 Urgent Return
Denver Gas Line Houston Shop
MTR-014 (1 item)
ETA: Apr 24, 8:00 AM
Reason: Motor Failure - Needs Immediate Repair

Upcoming Mobilization Schedule

Date Job Equipment Status Carrier
Apr 26 Phoenix Water Main Full BHA + 2 Reamers Ready Hotshot - FastFreight
Apr 28 Denver Gas Line Replacement Motor Pending R&M Company Truck #8
May 1 Dallas Water Main Full BHA + 3 Reamers Partial - 2 items in R&M TBD
May 3 San Antonio Pipeline Full BHA Ready Company Truck #12

Business

Pipeline, financials, and job closeout tracking

$4.2M Total Pipeline Value
23 Active Opportunities
68% Win Rate (YTD)
$1.8M Awarded This Quarter
Prospect $1.2M 8 opportunities
Austin Energy
36" Gas Main Crossing
$285,000
2,100 ft Bid due: May 15
TxDOT
Highway 290 Utilities
$420,000
3,400 ft Bid due: May 22
City of Dallas
Water Line Replacement
$165,000
1,200 ft Bid due: May 28
Proposal Submitted $890K 5 opportunities
Kinder Morgan
Pipeline River Crossing
$340,000
1,800 ft Submitted: Apr 18
Hot
AT&T
Fiber Conduit Install
$185,000
2,800 ft Submitted: Apr 10
Enterprise Products
NGL Line Extension
$365,000
2,200 ft Submitted: Apr 5
Negotiation $680K 3 opportunities
Williams Companies
Interstate Crossing
$425,000
2,600 ft Decision: Apr 28
Hot
Centerpoint Energy
Distribution Upgrade
$255,000
1,900 ft Decision: May 2
Awarded $1.8M 7 jobs
Houston Pipeline Co
24" Transmission Line
$520,000
2,450 ft Start: Apr 14
Active
Dallas Water Utilities
36" Water Main
$385,000
1,650 ft Start: May 1
Scheduled
Phoenix Metro
Sewer Force Main
$445,000
1,800 ft Start: Apr 21
Active
Revenue (YTD) +18%
$3.2M
Target: $4.5M
Gross Margin +3%
34.2%
Target: 32%
Backlog
$2.8M
12 jobs scheduled
A/R Outstanding -8%
$485K
DSO: 34 days

Monthly Revenue

$600K $450K $300K $150K $0 Jan Feb Mar Apr May Jun Jul Aug Sep Oct ▲ Current

Invoice Status

Current (0-30 days) $285,000
Due (31-60 days) $142,000
Overdue (61-90 days) $48,000
Critical (90+ days) $10,000

Job Profitability (Active & Recent)

Job Client Contract Costs Margin Status
Houston Pipeline Crossing Houston Pipeline Co $520,000 $342,000 34.2% In Progress
Dallas Water Main Dallas Water Utilities $385,000 $95,000 Mobilizing
Phoenix Sewer Force Main Phoenix Metro $445,000 $198,000 38.1% In Progress
Austin Fiber Install Google Fiber $280,000 $265,000 31.8% Complete
Denver Gas Line Xcel Energy $365,000 $28,000 Standby
4 Awaiting Closeout
$185K Pending Retention
2 As-Builts Pending
$42K Change Orders Pending

Austin Fiber Install

Google Fiber
$280,000
Closeout Progress
85%
Final walkthrough
Punch list complete
Final invoice submitted
As-built drawings Due: Apr 30
Retention release $28,000

San Antonio Crossing

CPS Energy
$195,000
Closeout Progress
60%
Final walkthrough
Punch list complete
Change order approval $18,500
Final invoice
As-built drawings

Midland Pipeline

Pioneer Natural
$425,000
Closeout Progress
95%
Final walkthrough
Punch list complete
Final invoice submitted
As-built drawings
Retention release $42,500 - May 15

Fort Worth Water

Fort Worth Water Dept
$310,000
Closeout Progress
40%
Final walkthrough
Punch list items (3) Overdue
Change order approval $23,500
Final invoice
Retention release $31,000

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