Control Tower
HDD Operations Overview
5
Active Jobs
3 / 2
Drilling / Reaming
45 / 23
Deployed / Available
8
Equipment Due Inspection
Active Operations
USARecent Activity
Houston Pipeline - Run 3 Complete
15 min ago
Denver Crossing - Reaming Started
2 hours ago
Motor MTR-015 - Inspection Due
4 hours ago
Phoenix Install - Job Complete
Yesterday
New route planned - Dallas River
Yesterday
Quick Actions
HDD Route Planner
Left click to add start point, way points and end point. Right click to finish before hitting View Cross Section
Route: 0 m
Buildings: 0
Waterways: 0
Roads: 0
Railways: 0
HDD Borehole Parameters
From horizontal (Inc: 78°)
Surface or underground
From horizontal (Inc: 102°)
Maximum depth below entry
Above bore path
Curvature limit
Curve shape
Plan View
Section View
Live Operations
Real-time monitoring of all active HDD operations
Houston Pipeline Crossing
Texas Energy Corp
45% Complete
Run
3
Days
12
MD
2,450 ft
ROP
125 ft/hr
Inc
12.5°
Azi
275°
TF
45°
Depth
35 ft
Denver River Crossing
Colorado Gas & Electric
78% Complete
Pass
2 of 3
Days
18
MD
3,200 ft
Pull
85 klbs
Hole Size
24"
Product
16" Steel
Phoenix Highway Crossing
Arizona Water Authority
32% Complete
Run
2
Days
5
MD
890 ft
ROP
95 ft/hr
Inc
8.2°
Azi
182°
TF
90°
Depth
22 ft
Dallas Creek Install
North Texas Pipeline
55% Complete - Waiting on Parts
Run
4
Days
15
MD
1,850 ft
Delay
2 days
Seattle Bay Crossing
Pacific Northwest Utilities
92% Complete
Pass
3 of 3
Days
22
MD
4,100 ft
Pull
120 klbs
String Builder
Configure drill strings and reaming assemblies
Components
12.25" PDC Bit
5-Blade, 16mm cutters
12.25" Tricone Bit
TCI inserts, sealed bearing
9-5/8" Mud Motor
1.5° bend, 400-600 GPM
MWD/Gamma Tool
Real-time surveys
Non-Mag Collar
31 ft, Monel
5" Drill Pipe
S-135, 19.5 lb/ft
Crossover Sub
4-1/2" IF x NC50
24" Hole Opener
Roller cone, 4-cutter
18" Lo-Torque Reamer
3-cone, reduced drag
Current String Configuration
5" Drill Pipe
2,232 ft
NM Collar x3
93 ft
MWD Tool
32 ft
9-5/8" Mud Motor
28 ft
12.25" PDC Bit
0.5 ft
String Specifications
2,385.5 ft
Total Length
48,250 lbs
Total Weight
12.25"
Max OD
3.5"
Min ID
4-1/2" IF
Connections
8-15k lbs
Rec. WOB
Engineering Calculations
Hydraulics, torque & drag, and pullback force modeling
Drilling Fluid Properties
ppg
sec/qt
cP
lb/100ft²
lb/100ft²
lb/100ft²
Borehole & String
in
in
in
in
ft
ft
Operating Parameters
gpm
psi
psi
in²
Hydraulics Summary
1,245
Pump Pressure (psi)
OK
168
Annular Velocity (ft/min)
OK
Good
Hole Cleaning
OK
9.6
ECD (ppg)
OK
Pressure Distribution
Total System Pressure:
1,245 psi
(255 psi margin)
Annular Velocity Profile
Friction Factors
-
-
String Properties
lb/ft
lbs
-
ft
Torque & Drag Results
12,450
Surface Torque (ft-lbs)
OK
38,500
Push Force (lbs)
OK
52,200
Pull Force (lbs)
OK
45,800
Rotate Off-Bottom (lbs)
OK
Torque & Drag vs Measured Depth
Product Pipe Properties
in
in
lb/ft
lbs
Pullback Conditions
in
x
ppg
-
Pullback Force Analysis
78,450
Total Pullback Force (lbs)
47% of Safe Pull
34,790
Pipe Weight Component (lbs)
-12,340
Buoyancy Effect (lbs)
28,500
Frictional Drag (lbs)
15,200
Hydrokinetic Drag (lbs)
12,300
Capstan Effect (lbs)
Pullback Force vs Distance
Safety Factors
Asset Management
Track equipment inventory and deployment status
45
Deployed
23
At Base (Ready)
12
Ready to Deploy
8
Due Inspection
5
In Repair
| Asset ID | Type | Description | Status | Location | Hours Run | Next Inspection |
|---|---|---|---|---|---|---|
| MTR-001 | Motor | 9-5/8" Mud Motor 1.5° | Deployed | Houston Pipeline | 245 | Apr 15, 2024 |
| MTR-002 | Motor | 9-5/8" Mud Motor 2.0° | Available | Houston Base | 180 | May 22, 2024 |
| BIT-015 | Drill Bit | 12.25" PDC 5-Blade | Deployed | Denver Crossing | 82 | - |
| RMR-003 | Reamer | 24" Hole Opener | Due Inspection | Houston Base | 420 | Overdue |
| GYR-001 | Survey Tool | Gyro Steering Tool | Deployed | Phoenix Crossing | 156 | Jun 1, 2024 |
| MWD-004 | Survey Tool | MWD Gamma | In Repair | Service Center | 512 | - |
| MTR-008 | Motor | 7" Mud Motor 1.15° | Available | Denver Base | 95 | Jul 10, 2024 |
Crew Planner
Manage crew assignments and scheduling across all active rigs
Crew Schedule - April/May 2026
Rig / Crew
Week of Apr 14
MTWTFSS
Week of Apr 21
MTWTFSS
Week of Apr 28
MTWTFSS
Week of May 5
MTWTFSS
Houston Pipeline
Drilling
Dallas Crossing
Reaming
Phoenix Water Main
Drilling
Denver Gas Line
Standby
Austin Fiber Install
Drilling
Driller
Locator
Helper
Crew Change
Repair & Maintenance
Tool tracking, R&M workflow, and equipment readiness
127
Deployed
+3 this week
14
In Inspection
Avg 2.1 days
8
Awaiting Parts
-2 from last week
11
In Repair
4 critical
6
In QC
Ready soon
23
Ready to Deploy
+5 this week
R&M Cycle Time (Days)
Return Transit
Inspection
Awaiting Parts
Repair
QC
Average Total Cycle:
9.4 days
-1.2 days vs last month
Critical Priority Items
MTR-004
9-5/8" Mud Motor
Urgent - Stator Damage
Needed: Houston Pipeline (Apr 28)
MWD-002
MWD Gamma Tool
Awaiting Board
Needed: Dallas Crossing (May 1)
RMR-008
24" Hole Opener
Bearing Replacement
Needed: Phoenix Water (May 3)
BIT-015
12.25" PDC Bit
Cutter Inspection
Needed: Austin Fiber (May 5)
Parts Inventory Alerts
Motor Stators (9-5/8")
2
in stock
Reorder placed - ETA May 2
MWD Pulser Boards
0
in stock
Backordered - ETA May 8
Sealed Bearing Assemblies
3
in stock
Reorder required
PDC Cutter Inserts
24
in stock
Stock OK
Returned from Job
5 items
MTR-007
Mud Motor
9-5/8" 1.5° Bend
Hours: 245
BIT-022
PDC Bit
12.25" 5-Blade
Footage: 2,450 ft
COL-011
Collar
Non-Mag 31'
Hours: 312
Inspection
4 items
MWD-003
Survey Tool
MWD Gamma
MTR-004
PRIORITY
9-5/8" Mud Motor
Suspected stator damage
Awaiting Parts
3 items
MWD-002
Survey Tool
MWD Gamma
Needs:
Pulser Board
ETA: May 8 (Backordered)
RMR-008
Reamer
24" Hole Opener
Needs:
Bearing Assembly
ETA: Apr 26 (In Transit)
In Repair
4 items
MTR-012
Mud Motor
7-3/4" 1.15° Bend
Stator Replacement
Tech: Carlos M.
75%
BIT-018
PDC Bit
9-7/8" 6-Blade
Cutter Replacement x4
Tech: David L.
40%
QC / Testing
2 items
MTR-009
Mud Motor
9-5/8" 1.5° Bend
Flow Test
Pressure Test
Final Inspection
MWD-005
Survey Tool
Gyro Steering
Calibration
Signal Test
Battery Check
Ready for Release
Ready to Deploy
6 items
MTR-006
Mud Motor
9-5/8" 1.5° Bend
QC Passed Apr 21
BIT-025
PDC Bit
12.25" 5-Blade
QC Passed Apr 20
RMR-003
Reamer
24" Hole Opener
Assigned:
Dallas Crossing
Ship: Apr 26
8
Outbound to Jobs
5
Returning to Shop
12
Scheduled Shipments
Outbound to Jobs
SHP-2024-0892
In Transit
Houston Shop
→
Dallas Crossing
MTR-006, BIT-025, COL-008 (3 items)
ETA:
Today 4:30 PM
Carrier: Company Truck #12
Driver: Tom Williams
SHP-2024-0895
Scheduled
Houston Shop
→
Phoenix Water Main
RMR-003, MTR-011, MWD-005 (3 items)
Departs:
Apr 26, 6:00 AM
SHP-2024-0898
Loading
Houston Shop
→
Austin Fiber Install
BIT-019, COL-015, COL-016 (3 items)
Departs:
Today 2:00 PM
Returning to Shop
SHP-2024-0890
In Transit
Houston Pipeline
→
Houston Shop
MTR-007, BIT-022, COL-011 (3 items)
ETA:
Today 11:30 AM
Reason:
Job Complete - Routine R&M
SHP-2024-0893
Urgent Return
Denver Gas Line
→
Houston Shop
MTR-014 (1 item)
ETA:
Apr 24, 8:00 AM
Reason:
Motor Failure - Needs Immediate Repair
Upcoming Mobilization Schedule
| Date | Job | Equipment | Status | Carrier |
|---|---|---|---|---|
| Apr 26 | Phoenix Water Main | Full BHA + 2 Reamers | Ready | Hotshot - FastFreight |
| Apr 28 | Denver Gas Line | Replacement Motor | Pending R&M | Company Truck #8 |
| May 1 | Dallas Water Main | Full BHA + 3 Reamers | Partial - 2 items in R&M | TBD |
| May 3 | San Antonio Pipeline | Full BHA | Ready | Company Truck #12 |
Business
Pipeline, financials, and job closeout tracking
$4.2M
Total Pipeline Value
23
Active Opportunities
68%
Win Rate (YTD)
$1.8M
Awarded This Quarter
Prospect
$1.2M
8 opportunities
Austin Energy
36" Gas Main Crossing
$285,000
TxDOT
Highway 290 Utilities
$420,000
City of Dallas
Water Line Replacement
$165,000
Proposal Submitted
$890K
5 opportunities
Kinder Morgan
Pipeline River Crossing
$340,000
Hot
AT&T
Fiber Conduit Install
$185,000
Enterprise Products
NGL Line Extension
$365,000
Negotiation
$680K
3 opportunities
Williams Companies
Interstate Crossing
$425,000
Hot
Centerpoint Energy
Distribution Upgrade
$255,000
Awarded
$1.8M
7 jobs
Houston Pipeline Co
24" Transmission Line
$520,000
Active
Dallas Water Utilities
36" Water Main
$385,000
Scheduled
Phoenix Metro
Sewer Force Main
$445,000
Active
Revenue (YTD)
+18%
$3.2M
Target: $4.5M
Gross Margin
+3%
34.2%
Target: 32%
Backlog
—
$2.8M
12 jobs scheduled
A/R Outstanding
-8%
$485K
DSO: 34 days
Monthly Revenue
Invoice Status
Current (0-30 days)
$285,000
Due (31-60 days)
$142,000
Overdue (61-90 days)
$48,000
Critical (90+ days)
$10,000
Job Profitability (Active & Recent)
| Job | Client | Contract | Costs | Margin | Status |
|---|---|---|---|---|---|
| Houston Pipeline Crossing | Houston Pipeline Co | $520,000 | $342,000 | 34.2% | In Progress |
| Dallas Water Main | Dallas Water Utilities | $385,000 | $95,000 | — | Mobilizing |
| Phoenix Sewer Force Main | Phoenix Metro | $445,000 | $198,000 | 38.1% | In Progress |
| Austin Fiber Install | Google Fiber | $280,000 | $265,000 | 31.8% | Complete |
| Denver Gas Line | Xcel Energy | $365,000 | $28,000 | — | Standby |
4
Awaiting Closeout
$185K
Pending Retention
2
As-Builts Pending
$42K
Change Orders Pending
Austin Fiber Install
Google Fiber$280,000
Closeout Progress
85%
Final walkthrough
Punch list complete
Final invoice submitted
As-built drawings
Due: Apr 30
Retention release
$28,000
San Antonio Crossing
CPS Energy$195,000
Closeout Progress
60%
Final walkthrough
Punch list complete
Change order approval
$18,500
Final invoice
As-built drawings
Midland Pipeline
Pioneer Natural$425,000
Closeout Progress
95%
Final walkthrough
Punch list complete
Final invoice submitted
As-built drawings
Retention release
$42,500 - May 15
Fort Worth Water
Fort Worth Water Dept$310,000
Closeout Progress
40%
Final walkthrough
Punch list items (3)
Overdue
Change order approval
$23,500
Final invoice
Retention release
$31,000
Settings
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